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3/22/26 yesterday went well

Testing the 10 robots yesterday went much better than expected. Going into It I had already found one head assembly that didn't work so I didn't have high hopes. It turned out that was the only one that didn't work though, and swapping out its microcontroller fixed it.


The only other problem I found was that some of the joysticks are drifting and need larger dead zones. This should be an easy fix; it just needs a variable at the top of Stewy.ino for tuning it.


The goal for today is to fix that problem and get the rest of the photos and videos I need for Stewy V2's release.


To do today:

  • Implement and test the dead zone variable

  • write down all the photos I want for the site

  • write down all the videos I need for the site and YT video

  • Take all the videos and photos

  • upload and organize the files

  • Add the photos to the site



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